From: Erik Andresen Date: Fri, 18 Dec 2015 19:43:53 +0000 (+0100) Subject: avr/motor_ctrl: lower Brown out level to 2.7V X-Git-Url: https://defiant.homedns.org/gitweb/?p=ros_wild_thumper.git;a=commitdiff_plain;h=281134cf696b5f8cf5ce642cec43d35ba0464e7f avr/motor_ctrl: lower Brown out level to 2.7V --- diff --git a/avr/motor_ctrl/fuses.txt b/avr/motor_ctrl/fuses.txt index 7671ff3..068ecb5 100644 --- a/avr/motor_ctrl/fuses.txt +++ b/avr/motor_ctrl/fuses.txt @@ -2,4 +2,4 @@ http://palmavr.sourceforge.net/cgi-bin/fc.cgi avrdude -p atmega32 -P usb -c avrisp2 -U lfuse:r:-:i -U hfuse:r:-:i -avrdude -p atmega32 -P usb -c avrisp2 -U lfuse:w:0x3f:m -U hfuse:w:0xc9:m +avrdude -p atmega32 -P usb -c avrisp2 -U lfuse:w:0xbf:m -U hfuse:w:0xc9:m